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| GLASAIR III BY BRIEN A. SEELEY, C.J. STEPHENS AND THE CAFE BOARD |
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| The fastest aircraft tested thus far
in the CAFE Foundation and EAA Aircraft Performance Report program, the Glasair III is a
high performance design. The prototype first flew in 1986. It was designed in the mid
1980's by Tom Hamilton, Ted Setzer, Bob Gavinsky and others at Stoddard Hamilton Aircraft,
Inc., the kit manufacturer. Lyle Powell also offered significant input in the design. An all-composite, kit-built, low-wing aircraft, the Glasair III uses tri-cycle retractable landing gear and a 300 horsepower Lycoming IO-540-K engine. Originally flown with a 23.3 foot wingspan, a later factory option offered wingtip extensions giving a 27 foot wingspan. Bill Stamm, an independent supplier, offered alternative wingtip extensions for a 25.8 foot span. These latter were adopted by Bob Herendeen for his airshow aerobatic version of the aircraft in order to enhance its climb and tight turning abilities. The Glasair III kit includes pre-molded fuselage skins, wing skins, spars, cowling and empennage made of fiberglass and Derakane vinylester resin. It also contains complete hardware for the entire aircraft structure including controls, fasteners, weldments, landing gear system, engine mount, windshield, etc. Stoddard Hamilton Aircraft receives high praise from their builders for their technical support. They provide a well planned, detailed Construction Manual and thorough Pilot's Operating Handbook with the kit for each aircraft. A PERFECT CANDIDATEChuck Hautamaki's Glasair III, N313CH, was selected for flight testing because of its lightweight, stock, plans-built airframe with an unmodified engine. It also was skillfully built to be straight and very smooth. Its engine had only 130 hours since overhaul and had recently shown 78/80 compression on all cylinders. Ted Setzer and Tim Johnson of Stoddard Hamilton Aircraft, Inc., concurred with the selection of this privately owned aircraft and assisted in this report by providing engineering data about the design. The equipment list of N313CH included a King KX-155 navcom, King KT-76 transponder, intercom, Vision Micro engine instruments, and an 18 lb automatic engine fire extinguisher system. Chuck acquired his Glasair III kit second hand from its original purchaser, Clark Pollard, an American Airlines pilot from San Mateo. He built it in his basement in Minnesota. He received excellent technical support from Stoddard Hamilton Aircraft, after paying a nominal transfer fee. "They treated me very, very well." He built the III in his basement, alone, except for some help with the wing closure, engine overhaul and sewing of upholstery. When Stoddard Hamilton changed to a graphite stabilizer on the Glasair III to achieve more flutter margin, they sent out new stabilizers to their builders at no charge. Chuck said, "SH also lightened up their parts substantially shortly after I got my kit, by improving the bagging process." This aircraft had only three small changes from the plans; a slightly smaller induction air inlet, a slight recontouring of the landing gear doors, and the use of a fixed rather than adjustable cowl exit size. After making the necessary flight test preparations, Chuck and his son, David, flew his Glasair III to the CAFE Foundation's test facility in Santa Rosa from his home base in Loveland, Colorado. Chuck's Glasair III was tested with both the original 23.3 foot wingspan, and then with the 27 foot wingspan. Each long wingtip weighed 10.9 lbs; each short wingtip weighed 2.1 lbs. The swapping of wingtips was a task requiring only 20 minutes. Thus, this report actually covers the flying qualities and performance of two different aircraft with distinct personalities. All of the tests were performed in a total of six flights during two days, November 9 and 10, 1996. All flights were made with pilot and one crew member/flight engineer, excepting the final flight which was performed solo with reduced fuel and long wingspan. The data presented here are derived from recordings using CAFE barograph #3 and pitot probe #2. The Lycoming power chart for the IO-540-K engine was used to derive the power settings. The fuel flow readings were made using the Vision Micro gauge on the aircraft's instrument panel, and it was known to be fairly accurate. The intense testing schedule did not allow equipping the aircraft with the CAFE Foundation's fuel flow recording system for these tests and fuel flow readings were not available during the short wingspan test. Jack Norris and Andy Bauer made a computation of the climb rate decrement caused by the barograph's wing drag and showed it to impose a climb rate penalty of less than 1%. Glasair IIISubjective ReportBY C. J. STEPHENSAm I Lucky . . . Or What? As test pilot for the CAFE foundation these past five years I have had the opportunity to fly many different airplanes. This experience has enabled me to learn what I like and don't like about various features of aircraft designs. A lot of that preference is due to personal taste but over time one learns how his "ideal" airplane would be designed and equipped. I was ecstatic when I learned that the next airplane to be tested by the CAFE foundation would be a Glasair III. Not only had I heard many good things about the kit manufacturer and the aircraft's performance, but I just happened to start building a GA III on the 4th of July this year. What an opportunity it would be to do a complete handling and performance evaluation while in the early stages of building my own. I hoped that the one presented for evaluation would be a good one that was built close to the plans specification. This next part proves beyond a doubt that I am extremely lucky. Not only was this Glasair III built without any builder design changes but the quality of construction was superb. From the first look at the plane to the last, as Chuck Hautamaki flew it back to its home in Colorado, it was a feast for the eyes; a work of art. On my initial introduction to N313CH words like "perfection", and "masterpiece" kept running through my mind. It was the smoothest, shiniest and best looking aircraft I had seen, inside and out. This one should become the bench mark of quality to which all builders should strive to attain. TWO WINGSChuck's Glasair was built with both the standard 23.3' wingspan and a set of longer wingtips which give a 27' span. The design of the longer wing tip makes it possible to increase the fuel capacity by putting 2.5 gallons of fuel in each tip, but Chuck chose to leave them dry. Not having fuel in the tips makes changing them quite simple. The 16% increase in wing span promised to provide some interesting comparisons in the flying qualities and performance. THE CHALLENGEThe test plan was to use the first day for preparation and the following two days for actual flying. The plan included evaluating the handling qualities with forward and aft center of gravity in both long and short wing configurations, then installing the CAFE barographs and measuring a variety of performance data on each of the two wingspans. Considering the limited time available and the two wing lengths it was to be a busy and challenging time for our small band of volunteers. ARRIVALThe plane landed at the CAFE test facility in the long wing configuration carrying the short wing tips in the baggage compartment. The first operation after arrival was to completely de-fuel the airplane to obtain an exact empty weight. The main fuel tank is in the wing forward of the spar, with an additional 5 gallon header tank forward of the instrument panel. The exact weight and center of gravity (CG) was determined using the in-floor electronic CAFE scales. Normally we would establish a CG of 15% aft of the forward limit for the most forward measurements, however, even with Otis Holt (right seat) carrying 20 lbs of lead in his flight suit ankle pocket and all of the baggage compartment ballast in the most forward location, we could only obtain a CG 48% aft of the forward limit. During flight the CG normally migrates aft due to the entire fuel supply being located forward of the spar. The main tank is continuous from tip to tip and connected in the center to act as one fuel tank. There are several baffling ribs throughout the tank with drain/vent holes to allow the fuel to travel to the center pick-up point. Refueling is a slow process requiring filling one side then the other and back again to top off the first side. The fuel fills into the various cavities slowly and care must be used to ensure a full fuel load is obtained. The design could also use a better method of grounding the aircraft during refueling. It has always bothered me a little to connect a static ground wire to the main gear of a fiberglass airplane expecting to get good enough conductivity to prevent a spark at the refueling point. During my initial conference with the owner, I asked many questions about flying his plane and reviewed some important numbers for use in flight. The information in the POH provided by Stoddard Hamilton was excellent and provided the valuable information for the flight preparation. PREFLIGHTChecking the oil and sumping the fuel was easy with the ports provided in the natural places. These small inspection holes, however, allowed little access to other components for detailed preflight inspection of the engine compartment and other areas of interest. Entry into the cockpit was accomplished by stepping up onto the back of the wing. As can be seen in the photos, the plane stands high on its main gear and requires a large step to get up onto the wing without stepping directly on the flap. This maneuver requires a little more than normal agility and leg strength. Due to the high shine and waxed surface, standing on the wing without sliding off was difficult at times. Note: Another Glasair III, built by Lyle Powell, features a nifty little step on the right side, below the entrance, which retracts by vacuum when the engine is started. About the only way to enter the cockpit is to step on the seat, sit on the seat back and then slip into the seated position. The seat back is very sturdy and the procedure is easy after you have done it the first time. The cockpit is roomy when compared to many homebuilts. I measured the instrument panel width to be 43" then walked over to a nearby Mooney for comparison and found it to be 41". I was very pleased with the general philosophy of construction of this test airplane. It was clean, well organized and simple. I think we all can learn a little from that concept. The seats were made of quality leather with fabric inserts and the head liner was Ultrasuede. The interior was finished in soft gray tones which seemed to enhance the spacious, comfortable feeling. The seat cushions were made of a firm foam which proved to be very comfortable. The leg wells were roomy enough to not be constricting and the good leg support made long flights very relaxing. The instrument panel was beautiful and well laid out for VFR flying. Across the top of the panel was a horizontal row of five Vision Micro engine instruments. The second and third instruments from the left were the manifold pressure and rpm. Since those two instruments are referred to so frequently I feel they should stand out more and not be buried in a row of other similar instruments of lesser importance. It is a matter of balancing function and aesthetics. If the panel were to be set up for IFR flying I feel that the flight instruments would need to be moved up more to the line of vision rather than having the engine instruments along the top. The radio stack was kept basic with one nice nav/comm and a transponder using a blind altitude encoder. All of the installed electronic equipment worked flawlessly throughout the flight testing. A simple tow bar was provided for ground handling and worked very well. The plane was light enough that one person can easily move it about on the concrete ramp. TAXIINGThe Lycoming IO-540 sprang to life and idled beautifully after a brief prime using the electric fuel pump. A first impression is that this is a big engine (300 hp) for such a small airplane and it gives off a beefy sound. The stock exhaust system was installed using no muffler. The noise level inside the cockpit however seemed quite normal and comfortable. Very little power was needed to start the Glasair moving quickly down the taxiway. Directional control is accomplished using light braking with the toe brakes. Brake pedals were only installed on the left side, although the factory makes an optional set available for installation on the right side. No cowl flaps were installed, however the oil temperature and the CHT remained exactly at the desired readings on all flights even during the sustained high performance climbs. There was no heat cuff installed for cabin heating or defog operation. Even while flying at altitudes of over 10,000' the cabin remained warm enough, probably due to engine heat and the oil cooler discharge air being directly in front of the cabin vent (right side) air intake. There was no outlet for any defog system, but a slight fogging problem encountered on the ground was quickly cured by opening an entry door momentarily. The gull wing cockpit entry doors were large, with a very simple and effective pin locking mechanism and gas struts to hold them open. With the engine running, the prop wash seemed to blow the doors around quite a bit. For that reason it seemed best to keep the door closed while taxing. On a windy day it would be even more important to taxi with entry doors closed to prevent damage to the door hinges. The fuselage sits level during ground operations which provides an excellent field of view. The pre-takeoff procedures were well sequenced and logical using the laminated checklist provided by the builder. The flaps stay full up and locked, or full down and locked but the two intermediate positions stay in position only if there is an air load against them. This is due to the way the locking device works on the manual flap handle located on the center console. The normal takeoff procedure is to use the first notch of flaps. Therefore, when awaiting takeoff clearance the flaps will sometimes increase to a higher setting. Prior to taking off it may be necessary to reset the flaps to their proper position. A more secure flap detent would be desirable to preclude possible takeoffs with the flaps in the wrong position. The only provision for re-trimming the plane from the cockpit was the electric pitch trim switch located on the center console at about the belt loop height. Having it located there made it awkward to operate. There was no pitch trim indicator installed; however, by looking back at the elevator counterbalance horn the trim could be easily set prior to takeoff. TAKE OFFAfter a quick mental review of the POH procedures and flight parameters it was time to get airborne for a look at the flying qualities. I had been advised that lift off should occur at about 90 mph IAS with the long wings. Chuck had also cautioned me about the possibility of trapping the main landing gear out if I delayed the gear retraction too long or climbed too shallowly at first. With the rapid acceleration and the relatively slow gear retraction it is necessary to control the airspeed until all of the landing gear indicators show full retraction. Liftoff occurred abruptly upon rotation at 90 mph as expected. Gear retraction was normal and since the speed was building rapidly, a slightly steeper climb was used to maintain less than 120 mph until all three lights were out. Although during the first flight the landing gear retracted normally, on one subsequent flight I did manage to trap the right main in the unlocked position. This situation was further compounded because the three red gear unlock lights are partially hidden behind the throttle knob and not easily seen from the left seat. During the short-winged flights, takeoff occurred at 96 mph and the airplane climbed in a more noticeably nose high pitch attitude. As indicated by the tabulated data, the rate of climb suffers during a climb when flying with the short wings. STATIC LONGITUDINAL STABILITYThe airplane was trimmed to level flight at Va (200 mph). Then, using the CAFE hand-held stick force gauge, I measured the pitch stick force at each 10 mph increment of airspeed change over the entire level flight speed envelope without re-trimming. This stick force gradient gives an indication of the aircraft's tendency to return to the trimmed airspeed. A flat stick force gradient (low stick forces) makes the plane harder for a pilot to fly since there is low control force feedback. This becomes even more important in an airplane such as the Glasair III due to the high airspeeds normally experienced where after even a brief period of distraction the aircraft will quickly end up considerably off airspeed and altitude. The test was repeated at the most forward as well as at the most aft center of gravity locations that could be reasonably obtained. Measurements were made flying with both long and short wings (see graph ). My opinion is that all figures obtained show that the Glasair has an excellent stick force gradient. There is a gradual and steady build-up of stick force as the airspeed is changed away from the trimmed speed. Even in the most aft configuration tested, the aircraft showed ample force. The graph shows the full results for comparison. DYNAMIC LONGITUDINAL STABILITYShort period damping characteristics were evaluated at 6,000' at 140, 170 and 200 mph IAS in the forward and aft CG configuration, using first the long and then the short wings. Both stick-fixed and stick-free situations were compared. The stick was held in neutral position during the stick-fixed and released during stick-free. The results were virtually deadbeat during all evaluations. Excellent natural stability certainly adds to the Glasair III's beautiful handling quality. Dutch roll oscillations were excited by synchronizing pitch/roll/yaw inputs together. The damping was immediate with no evidence of Dutch roll tendency when the test was performed using both wing tip configurations. Yaw damping was positive although usually two overshoot cycles occurred after rudder release. MANEUVERING STABILITYStick forces were measured as G forces were increased with the aircraft trimmed for level flight. The tests were conducted at 6,000' at Va (200 mph) and in landing configuration at 1.3Vs (117 Mmph). Measurements were made at both the forward and aft CG positions. As would be expected, the aft CG. produced lighter stick forces. The rate of stick force increase was linear with ample stick force present at the maximum G evaluated. The control forces felt light enough for good maneuvering yet had high enough feedback to assure accurate pitch control. ( See graph) ROLL RATESRoll rates were measured by timing the bank change from the video recording made during each flight. The change was measured from a 60 degree banking turn in one direction to a 60 degree bank in the opposite direction in approximately level flight. Full stick throw was used with no compensation made for the time it takes to accelerate to the roll rate; therefore the actual sustained roll rate would be in excess of that reported. Remember, the fuel is carried in the wings and we were performing the roll rate evaluations with a nearly full fuel load and with both seats occupied. The comparisons were accomplished with similar fuel loads on each flight. SPIRAL STABILITYSeveral tests were performed to explore the natural stability about the roll axis. First the plane was trimmed to level 30 degree bank turns and released. The times required for the plane to either increase, or decrease, the bank by 15 degrees was measured. In all cases the airplane displayed a slight (approximately 1 degree/sec) tendency to roll to the left. This seemed to be caused by an out-of-trim condition. The only cockpit trim available was pitch trim. I believe that, if the out-of-trim condition had been corrected, the plane would have remained in a continuous rate turn, exhibiting neutral spiral stability. The test was performed at both 200 and 117 mph. ROLL DUE TO YAWA test was performed maintaining level flight at 130 and 200 mph IAS with 1/2 rudder displacement, measuring the stick force required to hold the bank constant at a bank required to hold a constant heading. The exhibited dihedral effect should become more pronounced with slower airspeed or increased Angle of Attack. See table below. 130 MPH 2.0 lbs stick force 200 MPH 1.2 lbs stick force I also checked to see if the wings could be leveled from a 30 degree bank with the use of the rudder alone. In both directions at 160 mph it was possible to level the wings although during the right turn the recovery occurred more quickly, probably due to the torque of the engine and the slight out-of-rig condition. STALLSThis Glasair III had small stall strips installed on the leading edge of the wing near the root. During stall exploration I followed the advice contained in the POH by ensuring that I had plenty of altitude (8000') before attempting stalls. I also mentally reviewed the suggested spin recovery technique should an unintentional spin be encountered. Throughout the six flights I had the opportunity to perform many stalls with both wing lengths and with varying CG. locations. Every stall and recovery appeared to be exactly the same with the exception of one situation. The exception occurred on one of the later flights with the heavy barograph installed directly in front of the airflow of the aileron. In this situation as the airspeed was reduced, the aileron and rudder required to hold level flight increased so much that, just prior to stall, it became necessary to use full rudder and about 1/2 aileron. These abnormal inputs were caused by the installed CAFE test equipment. Even with this large amount of control input the stall and recovery characteristics were quite similar to the other stalls. All of the stalls observed reacted with very little airframe buffet or noticeable sounds until about 1 mph prior to the stall. Then one very noticeable shudder would take place and the stall would occur. At the stall the left wing would always drop about 20 degrees and the nose would pitch down noticeably but not uncomfortably. I feel the slight out-of-rig condition may have been the cause of the left wing drop. In every case the recovery was instantaneous and positive following the slight forward repositioning of the stick. Altitude loss was minimal and no secondary stalls occurred during any recovery. Even with the asymmetry evident during the barographed flights the recoveries were very predictable and comfortable. It should be noted that all stalls were preceded with a slow deceleration of less that 1 mph per second. Accelerated stalls were explored up to an airspeed of 110 mph with all of the same characteristics being displayed. A pronounced nose high attitude was required to maintain level flight during approaches to the stall in the short wing configuration. LANDINGSI was very interested in evaluating the approach and landings of the Glasair III since this high performance airplane has on occasion given a few pilots some difficulties. Field of view letting down and entering the pattern is good. Any blind spots can be eliminated through mild banking. The plane is noticeably faster than most airplanes in its class and planning the let down is a must or you will arrive at the airport either too high or too fast. The landing gear speed is 140 mph which seems adequate for most situations The airplane is clean and does not want to lose speed easily until the gear and flaps are extended. This is another reason to plan the descent carefully. Chuck explained that it was recommended to fully extend the flaps immediately after the gear extension on downwind. However, I felt that created a large drag change and neces- sitated a major power input to maintain level flight. My preference was to extend only 1/3 flaps right after the gear extension, then extend the remaining flaps just prior to starting the base turn. A pattern of 115 mph IAS works well with a target speed across the fence of 100 mph. Accurate control of the airspeed is necessary. This airplane has high performance and requires good discipline to fly it safely. On final it is extremely easy to hold the airspeed to the exact number that is targeted for approach and touch down. It has excellent power response when acceleration is needed and ample drag when deceleration is needed. With accurate control of the power and pitch on final, the airplane will touch down precisely where desired. An important item is to not "pull off" the power and expect the airplane to float to a landing. It shows its high spirited, high performance lineage and must be flown completely throughout the landing. It is not a difficult procedure but if you are not used to landing this way it will require some practice. The cockpit sensation gives the feeling that the airspeed is quite high during landing. Normally during my experience a landing roll of about 3,000' seemed to be the standard although shorter rolls could be attained with heavier braking. The stiff landing gear leaves no doubt when the landing occurs. Various types of descent profiles were explored and reported. (See table). It certainly was impressive to see rates of descent near 4,000 fpm and true airspeeds in excess of 300 mph. LONG WING/SHORT WINGA burning question that seems to be omnipresent is, "How do the different wings lengths compare?" The most noticeable differences are the greater climb rate with the long wings and the more nose high attitude at slow speeds with the short wings. At altitudes above 6,000', the long wing seems to win out as far as speed is concerned. As would be expected, the roll rates are faster with the short wings installed. The short wing fits into a smaller hangar. The landing speed with the short wing is faster, requiring greater runway length. Due to the Glasair III's high wing loading, the margin for pilot error during an engine-out approach to landing would be extremely small. The longer wing configuration would improve the emergency landing problem by reducing the landing speed slightly. Is it worth the effort to own both wing lengths? Considering that the interchangeable wing tip construction is actually a minimal amount of effort it is probably something that is worth doing. CONCLUSIONSThe Glasair III is a fine airplane with excellent flying qualities. It is not an airplane that is meant for the low time or inattentive pilot. The speeds and performance are outstanding. The builder who keeps his airplane light and simple is bound to be rewarded with excellent performance. __________ flight reports __________ |
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